The before-mentioned problems create a dangerous working environment for employees assigned to polishing tasks and an effort was made to find ways to reduce or eliminate these problems while still maintaining an economically profitable procedure and quality product. While at the company, I spent a great deal of time working with other individuals to try to combat the ergonomic shortcomings of the polishing procedures. Our efforts resulted in the implementation of club-holding fixtures, improved rest and stretch breaks, an effort to maintain machine cleanliness to reduce vibration, and more attention to be paid to early warning signs of cumulative trauma disorders.
Once the background data was collected, we sought to develop a fixture that would not only provide a better “handle” for the club but would also move in a way that could eliminate excessive wrist movements. The main concern was finding a way to produce our ideas, so the company designated an employee who was familiar with machining metal to make fixtures for the plant.
Using a cylindrical aluminum handle (diameter = 1.25 inches, length = 3 inches), we sought to modify the existing hosel-holding pin to add movement by adding a joint just above the handle with the pin mounted at a 90 degree angle to its base. Adjustable set screws in the handle were installed so employees could set limits on the joint’s movement at angles where their work was most comfortable (page H). Further development led to a “trigger” (using scrap pistol triggers produced in another plant within the company) to be mounted to the handle that led to a locking mechanism in the head of the fixture. By depressing the trigger with one’s thumb, the joint would rotate to a desired position and lock in place when the trigger was released. This innovation was well like by employees because it eliminated the problem of “flopping” joints.
Hosel pins were improved on the new fixtures as well. Original fixtures had simple, solid, thinning metal pins that clubs could easily slip onto and off of. This lack of holding ability caused workers to lose control of clubs, producing finishing blemishes from accidental contact with the polishing surface or upon impact with the floor in the case of the club coming completely off of the fixture. New, expandable pins were developed that held the hosel tightly. Instead of the club being able to spin on the pin as with the old pins, the new, expandable pins spin at their base while holding the club snugly. Although putting the club on and taking it off of the pin now requires more force, less strength is needed to hold the club steady while polishing. The later outweighs the former in this case, making the trade-off an ergonomical advantage. The ultimate judges, the workers, agree with this theory and are very happy with the new hosel pins.
The cylindrical aluminum handles of the fixtures were knurled to improve the employee’s grasp and in some cases, where workers were still bothered by vibration, or if the hard, metal handle aggravated their hands due to excessive gripping, the handles were turned down to a smaller diameter and covered with rubber pipe sleeves. This covering adds padding to the handle and the rubber dampens vibrations passing from the machine, through the club and fixture, to the hands of employees.
The company incurred hundreds of thousand dollars in compensation for repetitive injuries during the 1994 in the golf plant alone. Figures such as this are damaging both economically and reputation-wise and the company realizes that serious changes must continue in an attempt to provide employees with safer workplaces.
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